An internal investigation revealed that engineers knew of the problem but approved the design anyway, then later redesigned the switch to fix it but did not assign a new part number to the altered switch as required. They also lied about and covered up their actions. GM CEO Mary Barra fired 15 employees over the matter. But the company also has been criticized for taking years to act on the complaints, which it had received both from owners and from NHTSA.
The U.S. Justice Department’s criminal investigation, headed by the U.S. Attorney for the Southern District of New York, has been underway for more than a year. The question is whether it will prosecute individual employees for wrongdoing—which would be unusual—or just the company itself. In a statement released today, GM said it was “cooperating fully with all requests,” but had no further comment.
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